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The stabilized flow rate was 50.5 MMscfD on a 32/64" wellhead choke, with approximately 384 barrels of condensate per day. Last October the discovery well, High Island Block 24-L, ...
Re manufacturing, Manufacturing, repair and service: Wellhead & Valves,Christmas Trees, Choke Manifolds,1502 Chokes, Tee’s, Ells,Distribute BOP (Ram and Annular) We offer services from the ...
March 2025: production rate of 7.4 MMcf/d and wellhead pressure of 1,180 psi. 48/64" choke: August 2022 DST: production rate of 10.4 MMcf/d and wellhead pressure of 1,000 psi; versus; ...
Drilled to 5,440 m, the well tested 76 b/d of crude and 512 Mscfd of gas through a 32/64-in. choke with wellhead flowing pressure of 89-149 psi.
The well was spudded May 5 and reached 3,218 m TD. A successful drill stem test produced 400 b/d of condensate, with 24.3 MMcfd of gas flowing at a wellhead pressure of 2,450 psi on a 48/64-in. choke.
The city received a $4,500 wellhead protection grant from the state s Department of Environmental Quality, part of $677,000 total distributed throughout the state. By Josh Grosteffon ...
HOUSTON, February 24, 2025--OneSubsea and Innovex Sign Master Service Agreement for Subsea Wellhead Technology, strengthening long standing relationship.
Innovex International, Inc., a leading provider of products and technologies to the oil and gas industry, today announced the signing of a strategic Frame Agreement with SLB OneSubsea, for the ...
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