Proceedings World Geothermal Congress 2010
Bali, Indonesia, 25-29 April 2010
       Maintenance and Operational Experience Gained By Operating the Aluto Langano
                               Geothermal Pilot Power Plant
                                                           Merga Tassew
                        P.O. Box 1233, Addis Ababa, Ethiopia, Tel. 251-11-5512552, Fax.251-11-5525710
                                                      mergatassew@yahoo.com
Keywords: Geothermal power operation, geothermal                     output of 8.5 MW. The two high pressure wells LA-3 and
power plant maintenance, well output decline, Turbine                LA-6 are feeding the geo fluid to the conventional steam
derating, solid depositions,                                         turbine of the GCCU. The exhaust steam coming out of the
                                                                     steam turbine is delivered to a heat exchanger which, in
ABSTRACT                                                             turn, boils a binary fluid to drive the organic binary turbine.
Ethiopia is well endowed with geothermal resources, and              After its commissioning, the power plant operated for a
current exploration is believed to have studied only a               relatively short period of time before a number of problems
fraction of the ultimate potential. The potential prospective        arose that severely affected the availability and power
areas are distributed along the Ethiopian Rift valley system         output level, ultimately leading to the shutdown of the
which runs in a northeast direction along the entire length          power plant. These problems occurred underground, within
of Ethiopia. To begin to realize this potential, in 1998, the        the surface (fluid handling) equipment, and in the power
Ethiopian Electric Power Corporation (EEPCO) constructed             plant itself. After a number of years, EEPCO issued an
the Aluto Langano geothermal pilot power plant (8.5 MW               international tender to rehabilitate the power plant and put it
gross) consisting of two Ormat generating units, one an              back into operation.
OEC (Ormat Energy Converter) and the other a GCCU
(Geothermal Combined Cycle Unit consisting of a back
pressure steam turbine exhausting to an OEC bottoming
cycle unit) - each designed to have similar power outputs.
The power plant operated satisfactorily for a short period of
time right after commissioning before a number of
problems arose that severely affected its availability and the
power output level.
Repair and maintenance of the Aluto Langano GCCU has
been completed and the unit was put back into normal
operation in July 2007. During the original operational
period of the pilot plant and after its recent rehabilitation,
experience gained in operation and maintenance will
ultimately be used to develop and harness the huge
geothermal energy reserve exists in the rift valley region of
Ethiopia.
                                                                     Figure 1: Chart of Energy production before the failure
In the coming five years it is planned to expand the Aluto                  of the pilot plant
Langano geothermal field in two phases.
                                                                     Subsequently, EEPCO engaged the services of a geothermal
                                                                     consultant, Geothermal Development Associates, to do the
1. INTRODUCTION AND BACKGROUND                                       analysis of the problems and carry out the necessary repairs
The Aluto Langano geothermal field is located in the                 on the units to put it back into operation. Work carried out
Ethiopian main Rift valley, Lakes District, some 200 km              as part of the power plant rehabilitation includes:
south of the capital Addis Ababa, which is one of the
principal sectors of the East African Rift system. In this                ¾    Reconditioning of the GCCU steam turbine has
field detailed geological, geochemical and geophysical                         been completed and the unit is put back in
surveys were carried out during the late 1970's and early of                   operation. This included re-engineering of the
1980s. The result of the studies indicated that a high                         steam turbine to enable it operates at lower steam
temperature underground fluid exists with an evidence of                       pressures, upgrading the power plant automation
long time residence occupied by high temperature rocks.                        system (PLC) and improving the lubrication
Six deep exploratory wells were drilled at Aluto out of                        system of the steam turbine.
which four wells were successful to supply a geothermal
fluid to the power plant.                                                 ¾    Repair and maintenance (servicing and/or
                                                                               overhaul) of the wellhead valves has been
The ALuto Langano Geothermal pilot plant was built,                            completed.
commissioned and put into operation in 1998 to
demonstrate the potential of geothermal energy in Ethiopia                ¾    Flow tests, go-devil runs, and down-hole pressure
under a turnkey contract with Ormat International. The                         and temperature measurements to confirm the
power plant is composed of two generating units; the                           causes of the output declines were undertaken.
geothermal Combined Cycle Unit (GCCU), and the Ormat                           The result of the tests indicated that the two high
Energy Converter (OEC). Combined, they had a design                            pressure wells are in good condition and are
                                                                 1
Teso
            currently supplying the geothermal fluid to the                5.   Worn-out steam turbine shaft on the drive-end
            GCCU unit.                                                          side
       ¾    Installing data loggers to enable records of                   6.   Tube leaks in the OEC heat exchangers
            wellhead pressure and temperature under static
            and dynamic condition. This has helped EEPCO                   7.   Frequent failure of the cooling fan shafts
            personnel to understand the way the wells
            respond under dynamic flow condition.                     2.1 Solid Depositions in the Wellbore and Surface
                                                                      Equipment
       ¾    Analysis and investigation of corroded OEC heat
                                                                      Liquid dominated geothermal reservoirs are hydrothermal
            exchanger tubes to determine the root cause of the
                                                                      reservoirs that contain circulating liquids which transport
            tube failures. The result of the tests indicated
                                                                      the thermal energy of the hot rock with dissolved minerals
            brine carry-over, with traces of chloride, was the
                                                                      near to the surface by natural fluid circulation. The fluid
            root causes of the tube failure. Based on the
                                                                      comes from such reservoirs may form scale that deposits in
            results obtained it was decided to replace all the
                                                                      the well bore and fluid carrying surface equipment,
            heat exchanger tubes (over 2,000 tubes) with
                                                                      particularly after boiling and brine separation. Therefore the
            higher quality duplex stainless steel. Modification
                                                                      brine scaling potential, corrosiveness, non-condensable gas
            work is currently underway to install a duplex
                                                                      (NCG) and hydrogen sulfide (H2S) content are the four
            filtering system to remove any debris and solid
                                                                      major chemical characteristics that have to be studied and
            carryover to the heat exchangers in order to
                                                                      addressed in the geothermal power plant design.
            maintain fluid quality.
                                                                      The schematic diagram showing common locations of solid
2. IDENTIFIED PROBLEMS RELATED TO THE                                 depositions (Teso Merga report, 2001, UNU- GTP) shows
STEAM FIELD AND THE POWER PLANT                                       in Figure 2.
Some of the problems that were identified that relate to the
steam field and the power plant are:                                  The geothermal reservoir that feeds the well bore contains a
                                                                      variety of dissolved minerals and gases. Tests and
       1.   Solid deposition in the well bore and surface             downhole logs conducted on the Aluto Langano geothermal
            equipment                                                 field wells indicated that well LA-4 exhibited calcite scale
                                                                      depositions. This well was drilled in 1983 to a depth of
       2.   Well output decline                                       2062 m in the outflow zone of Wonji fault. The logging
                                                                      result of May 2006 indicated that a go-devil of 3 in
       3.   Difficulty of operating the two high enthalpy,            diameter stopped at a depth of 1085 m and a 4 ½ in go-devil
            wells LA-3 and LA-6 in parallel                           stopped at a depth of 1050 m while logging fragments of
                                                                      white soft pieces, resembling calcium carbonate, were
       4.   Journal bearing failure of the steam turbine              recovered from both go-devils.
                              Figure 2: Flow diagram showing common locations of solid depositions
                                                                  2
                                                                                                                            Teso
The blockage observed in well LA-4 has also significantly           available locally who could do the de-staging. De-staging
reduced the flow from this well. Subsequently, a well work          of the GCCU unit was performed successfully and the unit
over was recommended to remove the obstruction and bring            was put back into normal operation in June 2007.
the well back into normal flow. It is expected that, within a
six month time period, the well work over will be
completed and the well will come back into normal
operation.
3. RECOMMISSIONING OF THE GEOTHERMAL
COMBINED CYCLE UNIT (GCCU)
During early operation following commissioning the
GCCU, it was observed that when well LA-6 was opened
and the flow from both LA-6 and LA-3 wells was joined,
the LA-3 wellhead pressure increased while the flow of
LA-3 dropped sharply. This indicates that when the two
wells operate together, LA-3 was unable to flow sufficient
steam at higher system pressure to maintain a stable flow to        Figure 3: Plot of GCCU unit Energy Production
the unit. This issue was discussed in detail with the
Consultant and it was believed that the production pressure         Note: The unit was out of operation during the period of
of the wells was not sufficient to spin the multi-stage steam       April to August due to a reduction gear box failure (RG)
turbine.
                                                                    During the course of its operation after the rehabilitation,
Destaging of the steam turbine, to enable operation of the          routine vibration measurements revealed a gradual increase
GCCU at a lower inlet pressure, was suggested by PB                 in the vibration levels nearly 9 months after the start of
Power in its final report prepared in 2000. According to PB         operation. It was later discovered that the root cause of the
Power, by de-staging the GCCU unit and removing turbine             vibration was related to loosening of the inertial masses on
stages, the design steam inlet pressure would be lowered.           the pinion gear of the speed reduction gearbox. From the
This would match the stable production pressure of the              month of March to August 2008 the unit was out of
wells to the turbine’s capacity.                                    operation in order to rectify the problem with the reduction
                                                                    gear box (RG). The purpose of the RG is to couple and
The predicted performance of the GCCU unit was as                   reduce speed of the high speed steam turbine to match that
follows (from the original PB POWER design):                        of the synchronous generator.
                                                                    Extensive investigation on the cause of the gearbox
Table 1:                                                            problem was carried out. Information was also obtained on
                                                                    experience with gearboxes at similar geothermal power
    Steam Pressure inlet (bar)    Steam Flow      Power
                                                                    plants (such as the Puna, Hawaii plant). A repair strategy
         to the demister           Rate (t/h)     output
                                                                    was developed and the gearbox pinion was sent to the
                         12.0         29.0          4.0             Ethiopian Airlines workshop for reconditioning. Ethiopian
                                                                    Airlines reconditioned the RG and carried out dynamic
      Design data        10.0        24.05         3.25             balancing to acceptable industry standards. The RG was
      before de-                                                    subsequently taken to the power plant, installed and the unit
       staging            7.5         18.1          2.3             restarted and put back into operation in August 2008.
                          5.0        12.15         1.35             4. TUBE LEAK OF THE HEAT EXCHANGER OF
                                                                    THE OEC UNIT
                          7.0         26.8          2.9             The Ormat Enegy Converter (OEC) is an organic turbine
                                                                    that uses N-Pentane as a working fluid. The two medium-
    With first stage      6.0         23.0          2.5
                                                                    enthalpy wells, LA-4 and LA-8, are the primary energy
      removed
                                                                    source to boil the organic fluid in the tube and shell heat
                          5.0         19.2          2.1
                                                                    exchangers. The OEC unit is comprised of a one pass
    Removal of the        5.0         29.0          2.6             vaporizer and four stages of pre-heaters; the heat exchanger
    first two stages                                                tubes were made of 316L and duplex stainless steel except
                                                                    for the first and second passes of the preheater which were
          Actual         5.14        ~29.0         3.05             made of carbon steel.
    performance of
        the steam                                                   Approximately one year following the original
      turbine after                                                 commissioning of the OEC unit, in December 1999, a
    removal of the                                                  pentane leak was observed through the non condensable gas
    first two stages                                                (NCG) vent and caused the stoppage of the OEC unit. The
                                                                    results of investigations carried out subsequently indicated
                                                                    that pentane had leaked into the geothermal fluid stream
                                                                    due to vaporizer tube failure.
Based on the above and the actual flow tests conducted by
the rehabilitation consultant (Geothermal Development               During the recent rehabilitation of the Aluto plant, in order
Associates - GDA), it was recommended to remove the first           to investigate the root causes of the tube failures, samples
two stages of the rotor. The modification of the turbine            of the failed tubes and other relevant materials were sent to
rotor was implemented by shipping it to Conhagen                    a metallurgical testing company in the USA to carry out a
workshop in Texas, USA, as there were no workshops                  failure analysis. The company, Jonas Inc., conducted
                                                                    metallurgical analysis of the tube material and compatibility
                                                                3
Teso
of the chemistry of the geothermal fluid with that of the                       logic controller (PLC), Supervisory Control
tube materials.                                                                 Acquire Data Acquisition (SCADA) system and
                                                                                Human Machine Interfacing (HMI) of the power
                                                                                plant.
Table 2: Results of tube inspection
                                                                      6. CONCLUSION
    Tube       Number of        Pit Depths    Pit Diameter
               pits per foot       (mm)           (mm)                As described above, Ethiopia is endowed with considerable
                  on ID                                               geothermal resource potential. But, up to now, only a tiny
                                                                      fraction of this enormous resource has been used. The
        1           12          0.2 to 0.9       0.2 to 1             success with the re-commissioning of the Aluto plant will
                                                                      now pave the way for future expansion of power generation
        2           23          0.2 to 0.9       0.2 to 1             at Aluto and at other geothermal prospects.
        1           8           0.2 to 0.9       0.2 to 1             Bringing the Aluto Langano geothermal power plant back
                                                                      into operation has been a high priority for EEPCO in order
                                                                      to maximize the return on the capital invested in the project,
                                                                      provide power to the national grid system, and
The result of Jonas’ investigation indicated that localized           demonstrates that geothermal power from Aluto site as well
pitting inside the tubes was due to high concentrations of            as from other fields can reliably meet the future electricity
corrosive impurities carried into the heat exchanger by               demand in Ethiopia.
brine carry-over during the initial operation of the plant.
Jonas concluded that the heat exchanger material was not              Expansion of the Aluto Langano geothermal site to larger-
compatible with the chemistry of the Aluto wells. It further          scale power generation is in the pipe line and the experience
indicated that if the heat exchangers were operated under             gained in operation and maintenance of the existing pilot
the same conditions, further damage would occur to the                plant will ultimately be used for larger scale development.
heat exchanger tubes. The recommendation was to replace
the existing heat exchanger tubes with a more resistant               Close monitoring of the resource (reservoir performance,
grade 2205 Duplex Stainless Steel.                                    fluid chemistry and steam quality) and performance of the
                                                                      power plant will ensure the reliable operation of the pilot
5. EXPERIENCE GAINED                                                  plant as well as provide useful operational data that can be
                                                                      used for future power plants in the country.
    1. Experience gained in refurbishment of wellhead
       master valves and bleed lines is very important.
       This included experience with the assembly and                 ACKNOWLEDGEMENTS
       disassembly of master valves, hydrostatic testing,             My deep thanks to my company for granting me permission
       acquisition of spare parts, use of specialized tools           to present this paper on World Geothermal Congress
       and equipment, and local manufacture of some                   (WGC) 2010 conference. I also thank the Aluto Power
       valve parts.                                                   Plant Manager for providing me energy data to include into
                                                                      this paper.
       2.   The knowledge acquired in steam field resource
            management and wellhead equipment operation               REFERENCES
            would ultimately be used for Aluto expansion and
                                                                      Consultant Report (Geothermal Development Associates,
            other geothermal prospects.
                                                                          GDA) submitted to EEPCO, as per the Contract
       3.   Experience was gained with the operation of a                 Agreement (RHGP 1/97, June 2006) - Consultancy
            new, digital, Kuster K-10 tool for down hole                  services and Repair of the Alutoto Langano GPP.
            pressure and temperature logging.                         Jonas Inc. Report: Analysis of Heat Exchanger Tube pitting
                                                                          Aluto OEC -Unit, unpublished.
       4.   Knowledge was acquired in the use of wellhead
            data loggers and interpretation of the logged data.       PB POWER, Unpublished Report submitted to EEPCO:
                                                                         Aluto Langano Geothermal Pilot plant Project, June
       5.   Experiences was gained with the refurbishment of             200.
            cooling tower fans, specifically, in vertical shaft
            alignment, and correct tensioning of the torque           Geothermal Development Associates: Final Project TOR
            transmission belt, which will be used to resolve              Reports, November 16, 2007 and April 1, 2008.
            problems that may arise with the cooling system.          Teso Merga, 2001: Effect of Solid Depositions and
                                                                          Methods of control. UNU - GTP, Iceland, Report 9.
       6.   Knowledge was acquired in updating the power
            plant automation system. This familiarized plant
            personnel with the operation of the programmable