Scale Remover
Scale Remover
December 2018
Electrochemical Water
Treatment for Cooling Towers
Gregg Tomberlin
Jesse Dean
Michael Deru
Disclaimer
This document was prepared as an account of work sponsored by the United States Government. While this
document is believed to contain correct information, neither the United States Government nor any agency
thereof, nor the National Renewable Energy Laboratory, nor any of their employees, makes any warranty, express
or implied, or assumes any legal responsibility for the accuracy, completeness or usefulness of any information,
apparatus, product, or process disclosed, or represents that its use would not infringe privately owned rights.
Reference herein to any specific commercial product, process or service by its trade name, trademark,
manufacturer, or otherwise does not constitute or imply its endorsement, recommendation or favoring by the
United States Government or any agency thereof, or the U.S. Department of Energy’s National Renewable Energy
Laboratory. The views and opinions of authors expressed herein do not necessarily state or reflect those of the
United States Government or any agency thereof or the National Renewable Energy Laboratory. Funding provided
by the U.S. General Services Administration.
The work described in this report was funded by the U.S. General Services Administration and the Federal Energy
Management Program of the U.S. Department of Energy under Contract No. IAG-11-01815 and Task No. 10438-
01.01.02.
Acknowledgements
United States General Services Administration (GSA) Region 4: James Lackey, Joseph Swinson, Todd Kronlein,
Cameron Kaminsky, Roger Blakley, Tim Sherrod and Douglas Baughman
GSA GPG Program: Jay Fine and Kevin Powell
National Renewable Energy Laboratory: Michael Deru, Alicen Kandt and Dylan Cutler
Tenfold Information Design Services: Andrea Silvestri
The technology was installed at the Juliette Gordon Low Federal Building located in Savannah, Georgia. The
building is approximately 242,000 square feet. The building has two cooling towers utilizing traditional chemical
water treatment for the cooling water circulating through the two chiller condensers.
Measurement taken at the site included the flow of makeup water to the cooling towers and the blowdown flow
rate from the cooling tower basins. Additionally, energy measurements include the electrical energy from the
chillers, chiller water pumps, condenser water pumps, cooling tower fans, and the energy used by the AWT skid
and slip stream pump.
1
https://www.fedcenter.gov/programs/eo13834/
Water/Sewer Metered water consumption > 25% makeup water savings Met – Water savings at 31.6%.
Savings Blowdown volume reduction
Metered blowdown > 75% blowdown/sewer
was 99.8%.
Energy Metered chilled water system > 10% chiller energy savings Not Met - No energy savings
Savings energy consumption
Maintenance Maintenance records for 100% reduction in added chemicals and Met - Chemical usage
Savings current cost of chemicals and decrease in maintenance costs, including eliminated. Mechanical
labor reduced costs for mechanical cleaning cleaning costs were reduced
Water Quality Water quality monitoring Water quality meets site-specific Met - Chlorides increased.
standards (may include conductivity, pH, Vendor claims not a corrosion
hardness, alkalinity, silica, chloride issue. Verification
anions, salt anions, sulfate anions, recommended. Other factors
phosphate, copper, iron, and biological in normal range
th)
Alternative Water Technology System for Cooling Tower Applications Page iii
It was anticipated that the primary cost savings for this technology would be water, electric energy, chemicals
and maintenance labor costs.
Testing consisted of a baseline period where data was collected prior to the installation of the AWT system. At
the conclusion of the baseline period, the AWT technology was installed and data was collected with the new
technology in service for comparison. The data acquired during the testing period was adjusted to account for
differences in ambient temperature and cooling system duty during the two test periods.
Water savings exceeded the target goal by removing solids in the AWT system and reducing the amount of
blowdown that would have been required to remove those solids. The baseline water consumption of the
system was measured from June 8,2017 to July 16, 2017 and the AWT water treatment system was monitored
from July 18,2017 to October 23rd,2017. The water consumption during the testing period was 639,280 gallons.
It was calculated that the amount of water that would have been consumed without the AWT system in place
was 934,772 gallons. The water savings from the AWT system is therefore, 31.6%. Water and sewer savings
were estimated to be $6,662 annually.
The quantity of blowdown during the baseline period was 77,817 gallons. It was calculated from this data that
the amount of blowdown that would have been discharged during the testing period without the AWT system in
place was 209,492 gallons. The actual blowdown during the testing period was 307 gallons, or a reduction of
99.8%.
AWT systems can save energy usage by reducing scale build up on condenser tubes. The savings can be
substantial as heat transfer is lessened exponentially as buildup on the surfaces occurs. In this case, the system
did not have buildup during the baseline testing and does not normally see any substantial fouling of condenser
water heat exchanger tubes. Consequently, the weather normalized energy usage from the baseline period to
the testing period were found to be negligible. Although the potential for energy savings was not proven, the
removal of a large amount of solids by the AWT reactor could potentially improve system cleanliness and create
energy savings.
During the testing period when the AWT system was operating, onsite chemicals were no longer needed to treat
the cooling tower water. After running the AWT system for over four months without injecting chemicals, the
system did not show any adverse effects. The normal buildup of biological growth in the cooling tower was
diminished according to the maintenance staff. The chemical savings were estimated to be $4,080 per year and
the reduced cleaning labor costs were estimated at $1,200 per year.
The total annual savings for the system is estimated to be $6,811 which includes costs for the vendor to service
and clean its system. The cost of the AWT system equipment was $28,340 including shipping. The largest
unknown remaining cost is the cost of installation. The total cost to GSA for this installation was $43,057. The
vendor estimates that the installation cost without the cost burden of the GSA procurement process would be
$15,000. While it is in the vendor’s best interest to quote a smaller installation cost, the simplicity of the system
and the minimal interface with the existing equipment would likely entail a lower installation cost than what was
realized. Procurement should be easier after multiple installations, as well. Per GSA’s request, NREL calculated
the economics at both values and at an interim average value of $29,029 to install the system. This technology
does not require further study and is ready for further commercial implementation. The payback periods for all
three cases are outlined in Table 2.
ANNUAL SAVINGS
Vendor’s O&M Contract Costs -$6,000 -$6,000 -$6,000
Cooling Tower Cleaning Savings $1,200 $1,200 $1,200
Water Savings $7,531 $7,531 $7,531
Chemical Savings $4,080 $4,080 $4,080
TOTAL ANNUAL SAVINGS $6,811 $6,811 $6,811
SIMPLE PAYBACK (Years) 10.8 6.7 8.7
SIR (Savings to Investment Ratio) 1.39 2.25 1.72
Vendor’s
Reactor
Figure 1. Piping Diagram of Cooling Tower System with AWT Reactor Skid
The two components that need to be measured to account for water savings are (1) water consumption and (2)
cooling demand of the building. Water consumption was measured via an onsite water meter and tracked on a
monthly basis for the whole building. Make-up water and blowdown were also directly metered and water
consumption was recorded on a daily basis for both the baseline and the testing period in this study.
The heat rejected was measured via the onsite building automation system (BAS) by monitoring the condenser
loop (cooling tower) supply temperature, return temperature and flow rates. The cooling load data was correlated
to hourly outdoor air temperature and humidity values to establish the amount of heat rejected by the cooling
tower as a function of outdoor air temperature. These values are established by trending the BAS output for the
chiller plant in the building during the period from June to July of 2017.
The water quality was analyzed through assessment of the water quality reports delivered monthly by the AWT
vendor, as well as monthly water quality reports provided by the site’s water treatment contractor. These reports
evaluated: conductivity, pH value, total hardness, alkalinity, silica, chlorides and cycles of concentration (CoC).
The goal of the AWT system is to not only conserve water in cooling tower operations, but to also deliver cooling
to each building as efficiently as possible. The impact of the improved chiller operation (due to reduced scale) or
reduction in cooling tower operation was quantified.
The AWT system evaluated in the report is a commercialized technology. Given its commercialized state, the
system evaluated in this report is at a Technology Readiness Level 8 2 according to NASA definitions.
2
https://esto.nasa.gov/files/trl_definitions.pdf
TRL 6 Prototype System Verified (System/process prototype demonstration in an operational environment).
TRL 7 Integrated Pilot System Demonstrated (System/process prototype demonstration in an operational environment).
TRL 8 System Incorporated in Commercial Design (Actual system/process completed and qualified through test and demonstration).
TRL 9 System Proven and Ready for Full Commercial Deployment (Actual system proven through successful operations in operating
environment and ready for full commercial deployment).
TRL 10 Program Management and Market Development/Support Activities
Alternative Water Technology System for Cooling Tower Applications Page 8
B. WHY WE STUDIED IT
Cooling tower-related water consumption is one of largest potable water loads within buildings in the United
States. A breakdown of water consumption in office buildings is provided in Figure 2 and shows that about 28%
of water use is associated with heating and cooling due to the evaporative cooling demands associated with all
water-cooled air conditioning systems and evaporative based air conditioners.
Cooling towers can be found in all states throughout the country, and this AWT technology could save water in
most if not all climate zones. Although the technology can save water in practically all climate zone, facilities
located in hotter climates with a cooling season that lasts for more than five-six months per year will have higher
cooling tower utilization and consequently have greater potential for cooling tower water savings.
Although the number of cooling towers in each GSA region is unknown, it is expected that each region has
numerous cooling towers that could assist in reducing water consumption for each GSA region.
3
https://www.epa.gov/watersense/types-facilities
Alternative Water Technology System for Cooling Tower Applications Page 9
II. Evaluation Plan
A. EVALUATION DESIGN
Common make-up water quality and local weather conditions allowed for comparison of baseline vs. the AWT
case (see section II.E for a detailed description of the technology). The principal variable that changed between
the baseline and the AWT Case was the quantity of cooling required and, therefore, the amount of heat rejected
(and water evaporated) by the cooling tower. The normalization of water savings to cooling demand allowed for
effective comparison of the AWT technology to standard water treatment technologies. It also enables the
estimation of savings for other buildings. With appropriate metering of the water consumption and cooling
demand at other GSA sites it is possible to predict potential water savings that may be achievable with the AWT
system assessed here.
This report addresses water, energy and cost savings associated with the AWT system, and the water quality
provided by the AWT system. To quantify the performance of the AWT system, metering equipment was
installed to measure data for inputs, outputs and delivered results. This data were used to model the overall
performance of the AWT system with respect to water use, energy use and water quality. This performance
based modeling approach enabled the comparison of AWT system to the baseline water treatment system using
the same framework. Using the data gathered from the baseline and the testing period, the performance
objectives were analyzed for compliance.
Energy Savings Metered chilled water > 10% chiller energy savings
system energy
consumption
Maintenance Maintenance records 100% reduction in added chemicals and decrease in maintenance
Savings for current cost of costs, including eliminated costs for mechanical cleaning is less
chemicals and labor than the annualized costs for cleaning and maintaining the new
system
Water Quality Water quality Water quality meets site-specific standards (attributes of interest
monitoring may include conductivity, pH, hardness, alkalinity, silica high
range, chloride anions, salt anions, sulfate anions, phosphate,
copper, iron, and biological growth)
Ease of < 2 days to install and commission one Positive feedback during interview with
Installation cooling tower installer
Time required to install & configure.
Labor associated with install
Operability Facility operators have no issues with Positive feedback during interview with
technology O&M personnel. Usability opinion of
facility operators
The two components that need to be measured to account for water savings are (1) water consumption and (2)
cooling demand of the building. Water consumption was measured via an onsite water meter and tracked on a
monthly basis for the whole building. Make-up water and blow down were also directly metered and water
consumption was recorded on a daily basis for both the baseline and the AWT case in this study.
The chiller energy used from each monitoring period was measured via the onsite data acquisition system by
monitoring the condenser loop (cooling tower) supply temperature and return temperature. The condenser loop
flow rate was determined from pressure drop readings across the condenser pumps. The cooling load data were
correlated to hourly outdoor air temperature and humidity values to establish the amount of heat rejected by
the cooling tower as a function of outdoor air temperature.
The water quality was analyzed through assessment of the monthly water quality reports. These reports
evaluated conductivity, pH value, total hardness and nitrites.
Water Quality
GSA has developed the water chemistry standards shown in table 5, as a guideline to determine the
acceptability of cooling tower basin water quality for a given water treatment technology. Operations staff and
water treatment technology vendors performed monthly monitoring of these parameters to characterize
performance of the system. It should be noted that adherence to these ranges is not the only indicator of a
technology’s success. The operation of a water treatment technology is unique and as the function of the
materials used in its design may result in water quality that falls outside the ranges defined in the project
specifications. These chemistry standards were established for guidance in this particular project location. In the
application of these criteria, a site should consider site-specific water quality constraints, whether due to
influent potable water or discharge permit limitations, and make selections accordingly.
B. INSTRUMENTATION PLAN
The goal of the instrumentation plan for this technology demonstration focused on metering water and
energy use of the building cooling towers and chillers. To develop this measurement, instrumentation was
added for the following data points described in Table 6:
Condenser water flow rate Pump differential pressure readings Remote indication capability
Blowdown flow rate FTB4600 series totalizing flow meter 1/2 inline PVC line
Blowdown conductivity Existing Site Meter (Lakewood Model 140 controller) Mounted in line. Tie into 4-20 mA output
Makeup water flow rate FTB4600 series totalizing flow meter 3/4 inline, replace existing meter
Chiller power (x2) CTs and watt-hour meter 3-400 A CTs, WNC- 3Y-480 wattnode
Cooling tower fan power (x2) CTs and watt-hour meter 3-50 A CTs, WNC- 3Y-480 wattnode
Chilled water pumps (x2) CTs and watt-hour meter 3-50 A CTs, WNC- 3Y-480 wattnode
Condenser water pumps (x2) CTs and watt-hour meter 3-50 A CTs, WNC- 3Y-480 wattnode
Ambient dry bulb temperature Vaisala HMP60 T&RH sensor with shield
Data logging equipment 3 Campbell Scientific CR1000 data loggers with cell
phone modem, required peripheries, and other
supplies
Photos of cleaning the AWT reactor are shown below. The left photo shows pulling the reactor anode (titanium
rod) from the reactor shell (cathode). The center photo shows the magnesium and calcium buildup on the anode
and the right photo shows the anode after cleaning. Cleaning of the reactor is easily accomplished by scraping off
buildup from the anode. No chemicals are used in the process.
D. METHODOLOGY
The effectiveness of the technology was demonstrated by comparing test data during a baseline demonstration
period with test data after the AWT system was installed. Testing was performed during the peak cooling season
when the chillers were operating on regular basis.
After all instrumentation was installed and tested, the data collection began for the baseline test period. The
demonstration test period with the AWT system installed began after baseline data had been collected. A schedule
using the months of June to July for the baseline period and July to October for the demonstration test period is
shown in Figure 5.
Baseline Testing Period Demonstration Testing Period
June 8, 2017 through July 16, 2017 July 18, 2017 through October 23, 2017
4
Average water costs of all 11 GSA regions for fiscal year 2017.
Alternative Water Technology System for Cooling Tower Applications Page 17
III. Demonstration Results
A. QUANTITATIVE RESULTS
Water Savings
To accurately assess the water savings from the AWT system, it was necessary to calculate pre-installation
cooling tower water usage. Makeup water and blowdown was metered prior to the installation of the AWT
system at the Juliette Gordon Low Federal Building from June 8 to July 16, 2017 in order to develop a baseline.
The AWT increased the CoC by modifying the conductivity setpoint on the cooling tower controller. The initial
setting was 680 microsiemens (μS). During the test period, the setting was raised to 1,400 μS and finally 2,500
μS. The figure below shows the metered data for the makeup water and blowdown along with the startup
time of the AWT system. As shown, there was a 99% reduction in blowdown after the installation of the AWT
system. The baseline CoC averaged 3.9. Once the AWT system was engaged, very little water was blown down
making the CoC increase into uncharted territory when using the water balance calculation. The high removal
of solids internally make this type of CoC calculation a less valuable indicator for comparison with other types
of technologies.
Linear regression is used to model the relationship between two variables by fitting a linear equation to
observed data. One variable is considered to be an explanatory variable, and the other is considered to be a
dependent variable. The baseline regression model was used to predict how much water the baseline system
would have used compared to the new system. A confidence interval of 95% was applied to the model to also
predict the savings estimates upper and lower bounds.
The first multi-variable linear regression model was created using the following input variables to correlate
hourly cooling tower make-up water usage as a function of chiller plant condenser ton hours or chiller plant
energy usage and outside air conditions.
• Outside Air Temperature (OAT) – hourly outside air temperature recorded from NREL’s onsite data
loggers
• Outside Air Relative Humidity (OA_RH) – hourly outside air relative humidity recorded from NREL’s
onsite data loggers
• Chiller Plant Electricity (Chiller_Elec) – hourly total chiller plant energy usage from a combination of
chillers, pumps and cooling towers, calculated based on NREL’s onsite data logger readings
• Chiller Plant Ton Hours (Chiller_Ton.Hrs) – hourly total chiller plant condenser ton hours, calculated
based on NREL’s onsite data logger readings
• Weekday/Weekend (Wkd_Wknd) – Each weekday was given a designation of 1 and each weekend day
and federal holiday was given a designation of 0 to account for days when the facility is unoccupied and
to account for its impacts on chiller energy usage and cooling tower make-up water usage.
COAT x COA_RH = coded outside air temperature times coded outside air relative humidity[ -1=min to
+1=max]
COAT x CChiller_Elec = coded outside air temperature times coded chiller electricity usage [ -1=min to
+1=max]
The linear regression model was selected to ensure that the explanatory variables used in the model have p-
values less than 0.05. The explanatory variables that had the highest statistical impact were coded chiller plant
energy usage, Weekday/Weekend, coded outside air temperature and coded outside air relative humidity,
which would all be expected to impact the hourly cooling tower make-up water usage. The adjusted R2 for the
model is 90.35% and the normalized root mean square error for the model is 6.24%. The coefficients for each
explanatory variable are provided in Table 7.
Table 7. Hourly Baseline Cooling Tower Make-up Water Linear Regression Model Coefficients
r squared 0.9035
Intercept 271.10
CChiller_Elec 228.55
WKD_WKND 16.26
COAT 72.67
COA_RH -59.52
COAT x COA_RH -68.88
CChiller_Elec x COAT -29.66
Figure 7. Hourly Baseline Period Cooling Tower Make-up Water vs Predicted Cooling Tower
Make-up Water Usage (kgals)
In the regression analysis, since the data available for 6/8/2017, was a partial day, the baseline period for the
regression analysis was 6/9/2017, to 7/16/2017, and the predicted hourly cooling tower make-up water usage
was output and compared to the measured data. For the entire baseline period, the cooling tower make-up water
usage was 301,438 gallons, and the predicted cooling tower make-up water usage was 301,535 gallons, with a
percent difference of the two of 0.032%, indicating a very good fit for the baseline model.
Using the prediction curves and applying the data, the make-up water usage for the post-installation reporting
period was 639,280 gallons and the baseline system was estimated to use 934,772 gallons, with a savings of
295,492 gallons for this period, or 31.6%. The estimated water usage for the baseline system using the lower
bound was 913,403 gallons and the estimated make-up water usage for the baseline system using the upper
bound was 956,142 gallons, representing a 30.0% and 33.1% savings respectively. Water savings averaged 31.6%
from the baseline testing to the test period utilizing the AWT system. Make-up water flows and regression analysis
parameters are shown below.
The site water use reduction for a full 12 months is estimated to be 1,133,857 gallons.
Energy Savings
Energy savings claims for the AWT system are based on the technology’s ability to remove scale from a system
that has existing fouling and to keep systems that normally foul from fouling between cleanings. Scale build-up on
heat exchanger tubes can reduce heat transfer substantially with only a thin layer of scale. This loss in heat transfer
results in higher energy use to achieve the desired performance. The ability to clean the cooling water enough
that it will diminish scale build-ups has the potential to create significant energy savings. The energy used in the
system was measured on all relevant components for both the baseline period and the testing period. There was
little or no change in energy consumption between the two periods of operation. The plant operating staff stated
that the condenser tubes do not show scaling under normal operations and there is only a small amount of
“dusting” on the tubes where material settles during shut down. Because the tubes are not fouled, there was no
opportunity to decrease fouling and save energy. Therefore, the results of the energy savings are deemed to be
zero, but the potential for energy savings may still exist where substantial condenser tube fouling exists.
Chemical Savings
The manufacturer of the AWT system claims that chemicals are not required when its system is in operation.
The baseline period utilized the normal chemical injection scheme that costs the site about $4,080 per year.
When the AWT testing period began, the chemical dosing systems were taken out of service and no chemicals
were used for the remainder of the testing. For this savings to be considered, the resulting water quality needs
to be in line with system norms and GSA standards. Additionally, inspection of the system after testing should
show no increase in algae build-up at the cooling tower fill and basin. The final inspection showed a reduction in
this biological build-up, allowing for a reduction in cooling tower cleaning frequency.
The only constituent that changed substantially was chlorides (Cl-). Chloride levels rose with the AWT system
from 92 ppm in the tower basin up to 400 ppm four months later. As the concentration of Cl- increases, stainless
steel corrosion can take place although levels below 1,000 ppm are generally not concerning. The AWT system
does leave a high concentration of calcium ions (Ca++) in the water which will mitigate corrosion issues. In order
to insure that this is not an issue, chloride levels should be monitored regularly and the use of corrosion coupons
or a corrosion monitoring device that uses linear polarization resistance (LPR) should be used in all systems.
B. QUALITATIVE RESULTS
Building staff were interviewed after the testing was completed to understand any qualitative changes in
operational or maintenance issues. Comments for relevant areas are shown below:
Ease of Installation
The AWT system consists of a skid with a small footprint. Setting the skid, wiring and plumbing are
straightforward. The system does require compressed air and the manufacturer of the AWT system initially
assumed that building air would be available for its use. It was communicated to the manufacturer of the AWT
system that tying into GSA building air systems is not allowed practice. Consequently, the manufacturer of the
AWT system purchased a compressor that was installed with the system. The installation is separate from the
main cooling system only treating a portion of the flow. If the skid can be located close to the cooling water
supply and return piping, the slip stream piping runs are short. The ties into the cooling water systems do not
take much time or expense. Maybe the most challenging aspect is getting the skid to the upper levels of the
building where the cooling towers are normally located. For the Juliette Gordon Low building, the skid was
about four feet long and a little over a foot wide with a height of about five and half feet. The equipment weighs
less than five hundred pounds dry. Most buildings are capable of handling equipment of this size without issue.
Site Safety
Site safety can be affected by several factors. With regards to the AWT system, no new safety hazards were
introduce by installing the skid and tie in points. Site safety is improved by the fact that chemicals will be removed
from the site. Chemical usage is a common safety concern for transportation, changing chemical tanks, storage
and feed systems. The removal of all chemicals will increase site safety for these reasons and the will eliminate
the potential for dangerous chemical spills.
C. COST-EFFECTIVENESS
The primary savings on the project were projected to be water, electric energy, chemicals and maintenance
labor costs; energy and water were anticipated to contribute the most savings. Water savings exceeded the
target goal by removing solids in the AWT reactor and reducing the amount of blowdown that would have been
required to remove those solids. Water related cost savings were estimated to be $6,662 annually.
Savings in energy can be realized when build-up on heat exchanger surfaces is removed or if build-up that
normally occurs does not occur due to the systems performance. The savings can be substantial, as heat transfer
is lessened exponentially as build-up on the surfaces occurs. In this case, the system did not have build-up during
the baseline testing and does not normally see any substantial fouling of heat exchanger tubes in the
condensers. This is the reason that no energy savings were observed in this time limited evaluation. The claimed
cleaning effect of the system was not given an opportunity to perform as the system normally runs clean. This is
not the case in all facilities and keeping the condenser tubes clean can have a dramatic effect on heat transfer
Chemical usage was eliminated during the AWT testing period. Lack of a biocide in the system might be a
concern but the AWT system claims to generate biocide. After running the AWT system for over four months
without injecting biocide, the system did not show any adverse effects. The normal build-up of biological growth
in the cooling tower was actually diminished according to the maintenance staff. Not only does this create
chemical savings, but the need to clean the cooling tower is estimated to be reduced by 50%. The savings
realized from the elimination of chemical usage and the supply contract will be $4,080 per year. These savings
are offset by the cost of the annual AWT maintenance contract estimated to be $6,000. This cost includes
quarterly site visits for inspection and preventative maintenance, including AWT reactor cleaning. The cost also
includes all consumables, water analyses and monthly water reports. Utilizing the manufacturer’s annual service
contract increases the system warranty from 10 years to 20 years.
The reduced cleaning labor costs will be about $1,200 per year. These figures account for the $6,000 annual cost
for the manufacturer of the system to care for and maintain the system. The costs for AWT support include field
trips to the site. The costs were calculated for site visits to Savannah, GA, but may vary for other locations due to
increased travel costs.
The cost of the AWT system equipment was $30,340, including shipping. The largest unknown remaining is the
cost of installation. The total costs to GSA for this installation was $43,057. The manufacturer of the AWT system
estimates that the installation cost without the cost burden of the GSA procurement process would be $15,000.
The simplicity of the system and the minimal interface with the existing equipment suggest a lower cost than
what was realized. Procurement could be easier after multiple installations as well. Per GSA’s request, NREL
calculated the economics at both values and at an interim average value of $29,029 to install the system. The
payback period for all three cases are outlined below.
The cost of water is a primary determinant in whether the economics are favorable. For this evaluation, an
average water price was calculated using the last 12 months of data available. Table 10 below shows the data
and the result of $6.64 per thousand gallons of water used. The costs shown include the price for sewer
disposal.
The cost of water and the overall water savings were added to Table 11, below, along with the other relevant cost
factors to develop a simple payback period in years. While the average cost of water at the site is $6.64 per kgal,
the average water cost across GSA regions is $16.76 per kgal. Additionally, the average water costs for GSA regions
has increased by 41% between 2014 and 2017. These higher costs and the propensity for escalation work to
substantially reduce the payback periods for the technology. A simple payback period was calculated for both
water rates as shown below.
ANNUAL SAVINGS
AWT O & M Contract Costs -$6,000 -$6,000 -$6,000
Cooling Tower Cleaning Savings $1,200 $1,200 $1,200
Water Savings 5 $7,531 $7,531 $7,531
Chemical Savings $4,080 $4,080 $4,080
TOTAL ANNUAL SAVINGS $6,811 $6,811 $6,811
Using Savannah Water Costs
SIR (Savings-to-Investment Ratio) 1.39 2.25 1.72
SIMPLE PAYBACK (Years) 10.8 6.7 8.7
Using GSA Avg. Water Costs
SIR (Savings-to-Investment Ratio) 3.74 6.05 4.62
SIMPLE PAYBACK (Years) 4.0 2.5 3.2
Table 12, below shows the payback period sensitivity to water costs using the costs above for the estimated
installation costs in the right hand column of Table 11.
5
Based on water cost of $6.64 per thousand gallons (kgal).
Alternative Water Technology System for Cooling Tower Applications Page 27
Table 12. Payback Sensitivity to Water Costs 6
6
Using interim install cost estimate from Table 11.
Alternative Water Technology System for Cooling Tower Applications Page 28
IV. Summary Findings and Conclusions
A. OVERALL TECHNOLOGY ASSESSMENT AT DEMONSTRATION FACILITY
GSA installed the AWT system in the Juliette Gordon Low Federal Building in Savannah, Georgia, to test whether
the technology could maintain adequate water quality while conserving water, saving energy, and reducing
operating costs. (The determination of adequate water quality was made based on a previously developed set of
benchmarks.)
The economics of the AWT system are shown in Table 11, above. The AWT system showed substantial water
savings at 31.6%. The potential for energy savings was not yet proven, although the removal of a large amount of
solids by the AWT reactor could potentially improve system cleanliness and create energy savings.
Implementation decisions should not be made on the assumption of energy savings until further evidence is
shown.
Calculating the water reduction based on chiller load (gals/ton-hr) provides a metric for comparison to other
facilities. The evaporation portion can be calculated with the equation:
𝐹𝐹 × 𝑄𝑄
𝐸𝐸 =
∆𝐻𝐻𝑣𝑣𝑣𝑣𝑣𝑣 × 8.34 𝑙𝑙𝑙𝑙/𝑔𝑔𝑔𝑔𝑔𝑔
• 𝐸𝐸 is the gallons of water evaporated
• 𝐹𝐹 is a factor expressing the ratio of latent to sensible cooling (usually a value between 0.75 and 1,
with a value of one dictating total latent cooling)
• 𝑄𝑄 is the cooling required by the tower (can be calculated using 𝑚𝑚̇𝐶𝐶𝑝𝑝 ∆𝑇𝑇)
• ∆𝐻𝐻𝑣𝑣𝑣𝑣𝑣𝑣 is the latent heat of vaporization of water (approximately 1000 Btu/lb at sea level and
closer to 976 at Denver’s altitude).
If 𝑄𝑄 is set to be 12,000 Btu (or one ton), the lower limit for gallons per ton-hr can be calculated as between 1.10-
1.32 gal/ton-hr. (depending on 𝐹𝐹, the portion of cooling that is latent vs. sensible). The equivalent ton on the
cooling tower side rejects 15,000 Btu/hr due to the heat-equivalent of the energy needed to drive the chiller's
compressor, in which case the lower limit for condenser side gallons per ton-hr is 1.375 to 1.65 gal/ton-hr.
The key variable in the economic calculations is the installation cost. The costs for a GSA installation are higher on
the first installation than subsequent installations due to unfamiliarity with the system and the nuances associated
with the install. The costs for this installation totaled $73,397 for skid mounted equipment that only cost $28,340.
This ratio of installation costs to capital cost is high by industry standards. It is assumed that the costs for
installation could drop substantially for future installations. Further investigation into the cost breakdown for this
installation could reveal areas where money could be saved.
C. DEPLOYMENT RECOMMENDATIONS
Cooling tower performance depends on a variety of factors, many of which are location specific. Variables such as
ambient air quality are specific to the site location and tower location on the site (e.g. airborne particulate matter),
and seasonal changes have the potential to affect the observed operation of each technology evaluated. These
factors can contribute to biological growth or mineral deposits that require additional chemicals.
Given that cooling tower performance is a function of wet bulb temperature, cooling tower performance and the
amount of cooling delivered for each technology will also vary by site. Sites in dry climates with low wet bulb
design temperatures are favorable for evaporative cooling systems. Variability in technology performance may
also be a function of the type of cooling tower being used. The footprint of a given technology may vary with
respect to the cooling tower size, and may impact the feasibility of its installation.
As important as the quantity of water used is the cost of water at the facility. Water cost savings is equal to the
gallons saved times the cost per gallon. Areas with high water costs are of special interest.
Potable water quality is highly variable across the United States. The performance of these technologies is a
function of the quality of influent water that is treated. Locations with high hardness, pH or TDS values typically
have higher water and chemical usages. These are the sites that also have the greatest opportunity for savings.
The AWT system is well suited for both retrofit and new construction applications.
Rebate opportunities may be available through local water utilities to implement water conserving technologies.
The availability of these financial incentives can make the technology implementation even more cost effective.
Figure 8. Modeled water evaporation and blowdown savings across ASHRAE climate zones
The water savings numbers were then translated into annual cost savings using site specific water rates. Combined
water and sewer rates were obtained from an article published by American Water Intelligence based on a survey
of water and wastewater rates in 50 U.S. cities in 2012. The annual water savings for each location were multiplied
by the combined water rate for each city. The results from this analysis are presented in Figure 9. The wide
variation in water costs between the different cities results in a significantly different picture in cost savings than
Alternative Water Technology System for Cooling Tower Applications Page 31
is seen in water savings. Cities with high water rates (such as Atlanta, GA) generate the largest annual cost savings
despite not having the largest total water savings.
City
To gain an appreciation of the market potential for GSA, approximate system costs were utilized to calculate a
simple payback for each city. The paybacks denoted here are a very rough estimate, considering the assumptions
that the original system was operating at 3 CoC, the new system would achieve 15 CoC and that the annual
operating costs remain the same pre- to post-install, yet they give a feeling for the critical variables driving
economic viability of the system in various U.S. locations. The simple paybacks for a high installed cost assumption
($60,000) and a low cost assumption ($40,000) are shown in Figure 10.
Figure 10. Simple payback period for same system in evaluated locations
The buildings that have a large number of cooling degree days, high evaporation rates and poor water quality can
expect maximum water savings, whereas buildings in areas where typical wet bulb temperatures approach dry
bulb design temperature (high humidity) will generally see less water use and, therefore, less water savings. The
locations that have high water costs in addition to high water savings will result in the most economically favorable
locations for GSA to pursue in its deployment of AWT systems. It is also important to consider the water quality
of the locations under consideration.
Water Savings
To accurately assess the water savings from the AWT system, it was necessary to obtain (or calculate) both pre-
and post-retrofit water consumption. It is also necessary to have these consumption values for the same cooling
demand so that the savings can be normalized for weather variation. The weather normalization ensures that a
cooler or warmer than average month does not impact the calculated water savings.
Due to the fact that the temperature differential (∆𝑇𝑇) was calculated on the condenser water loop (not the chilled
water loop), it excludes any impacts of chiller efficiency.
The heat rejected was calculated for each 15-minute time step and then summed over the course of the day. Daily
values were also calculated for: average outdoor dry bulb, average relative humidity, minimum dry bulb,
maximum dry bulb, and operating hours. Each of these variables (plus weekday/weekend status) was tested for
correlation with the calculated cooling demand. The two significant variables identified were average outdoor air
temperature and weekday/weekend (expressed as a -1 for weekend and 1 for weekday). These correlations were
then able to be used to calculate make-up water for the building for historical periods where the BAS trend data
was not available.
The data is shown in Figure 11. The regression equations shown on the graphs are the equations used to correlate
cooling demand to operating conditions.
(kgals)
(kgals)
B. ECONOMIC ANALYSIS
The economic evaluation was based on the annual savings, the initial cost of the technology and the yearly
operation and maintenance costs. Using these values, the simple payback period (in years) was calculated.
Alternative Water Technology System for Cooling Tower Applications Page 34
The savings due to reduced water consumption were calculated using utility rates provided by GSA. It was
assumed that each gallon of water saved reduced the amount discharged to the sewer and subsequent costs
incurred by the site. This is due to the fact that the water saved due to improved water treatment technologies
was associated with the blowdown component of cooling tower water use. The blowdown, therefore, was not
required to be discharged to the sewer system, saving that portion of the water costs.
Cooling tower water use is made up of three components: evaporation, blowdown and drift. The evaporation
component provides the cooling to the chiller system and is not a function of the water treatment technology,
but rather by the cooling required by the building. The drift component is determined by the physical
characteristics of the cooling tower and the flow rate through the tower. Due to the fact that the cooling towers
(and their associated pumps) were not altered during the water treatment technology installations, the drift
component should not have changed from pre-to post-installation. Therefore, the water savings calculated in this
report should be direct reduction in blowdown due to the ability to increase the CoC achieved in the condenser
loop.
G. TECHNOLOGY SPECIFICATIONS
If the technology evaluation has been successful and the technology has potential for deployment within GSA,
GSA should support development of a technical specification that can use for procurement.