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To Sink and Swim

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0% found this document useful (0 votes)
17 views2 pages

To Sink and Swim

Uploaded by

Yasin Özdemir
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
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MIT OpenCourseWare

http://ocw.mit.edu

2.00AJ / 16.00AJ Exploring Sea, Space, & Earth: Fundamentals of Engineering Design
Spring 2009

For information about citing these materials or our Terms of Use, visit: http://ocw.mit.edu/terms.
The Task Motors
Design and construct a remotely Operated Vehicle that can To Sink and Swim In selecting motors and propellers the goal was to keep
power consumption down while still generating sufficient
be used underwater for exploration with video capabilities
and sensors for measuring environmental data. force to keep the vehicle relatively quick and
maneuverable. Two 500 gallon per hour (GPH) bilge pump

Constraints Foundations of Engineering Design 2.00A/16.00A motors were selected for the horizontal
(forward/backward) drive. They were positioned on the
•Maximum dimensions of 50cm x 50cm x 50cm vehicle so as to allow for a differential steering system. As
Sensor Package
•Topside control via 15m tether with 12V DC power the weakest motors available, they offered the lowest
•Maximum of three motors power consumption, but a pair of them provided plenty of
Syntactic force for forward drive.
•Submersible to a minimum of 20 ft. Foam
•Must have light bank, camera, and sensor package
A single 750 GPH bilge pump motor was used for vertical
drive. With only one motor operating in this axis, the extra
The Initial Design Drive power consumption was necessary to generate sufficient
In order to maximize the chance of success, the decision Motors Camera force.
was made to keep the design as simple as possible. We
used a rectangular PVC frame with a 30 cm square base and
20 cm height. Extra beams were placed along the bottom
Lift
Motor Light
Propellers
and the top to serve as attachment holds for the motors
and sensor package. Small holes were drilled in the PVC Banks To aid in propeller selection a series of tests were done to
piping to increase the rate at which they flooded with determine which models gave the best performance for
water. Weights (objects with greater gravitational force
than buoyant force) and floats (objects with greater
Testing and Variations from Initial Design power usage (see table below).

buoyant force than gravitational force) were arranged to Further tests showed that the use of a shaft extension
•In the first tests, propeller precession proved to be a significant issue. The phenomena reduced force paired with the white marine-style propeller gave force
self-right the vehicle and counter any unwanted rolls or
output somewhat and caused damage to the plastic connectors affixing the shaft extensions to the output superior to any listed in this table. However,
pitches.
motor shafts, including one catastrophic failure. Switching from hard plastic to nylon connectors, limitations in the test apparatus prevented exact figures
hammering the connectors further onto the motor shafts, and reducing shaft extension length from from being determined for comparison.
The three motors were placed near the bottom of the
10cm to 8cm reduced the prominence and negative effects of this behavior.
frame, two at the rear for x-y direction motion, controlled
by three-direction switches in the control box at the The initial decision was to use white-marine style
•The initial design lacked sufficient flotation and this was addressed in the short-term by adding two propellers with shaft extensions on all three motors,
surface. The lift motor was placed in the middle of the
extra buoys which were later replaced with blocks of syntactic foam. however, after repeated tests it was determined that the
bottom of the frame and controlled by button toggles at
the surface. The camera and two light banks were placed at force from the vertical drive motor with this arrangement
•The weight of the tether led to difficulty maneuvering in early tests. In order to address this, two was insufficient and was causing poor control, especially
the front. The sensor package was attached to the top, with
buoys were attached to the tether. The first roughly 1.5 m from the vehicle and the second roughly 2m when large amounts of tether cable were in the water (for
a float of similar size attached opposite for balance.
further up the cable. These provided a buoyant force that helped counter the weight from the tether. example, during deep dives). As a result, this propeller
This basic design served decently. Small adjustments were was changed to a very large, aircraft-type propeller which
•The initial lift motor mount plan was to use two long threaded rods in combination with a pair of had been found in tests to give excellent force output but
made throughout the process.
brackets to suspend the motor between two of the cross beams on the bottom of the device. This was at a high power cost. This extra power expenditure was
found to be both difficult and financially unfeasible so instead the decision was made to mount the ultimately deemed acceptable due to the vastly improved
Depth Tempera- Conductiv- Light (% motor directly to the rear cross beam then move the beam forward so the motor would sit at the performance with the new propeller.
center of mass.
(m) ture (C) ity (S/m) intensity
of •Perhaps the worst problem encountered in the final phases of testing was imperfect waterproofing Propeller Force Current
of the sensor pack. In early tests it was shown to leak quite badly from the end cap press fit points.
sunlight) These were sealed with a marine sealant, but further leaking through the threads of the screw-on cap 2 blade black midsize 1.3 lbs >5 A
were only addressed successfully with a combination of Teflon tape (to allow the cap to be screwed on
2.17 21.5 1.7 0.4 more soundly) and “monkey dung” (plumbers’ putty) sealant applied after shutting the cap, the latter
Small boat-style black 8.0 oz 2.3 A
1.32 20.8 1.8 0.5 of which had to be re-applied each time the cap was removed and replaced.

0.52 10.8 1.6 0.4 Diagrams, left to right: Small/med boat-style 11.0 oz 2.8 A

0.21 20.0 1.8 9.0 Self-righting


white
Precession
0.06 20.6 0 100 Motor Placement – Top View
(surface) Some Representative Data Motor Placement – Rear View White boat-style reversed 7.0 oz 2.1 A

Data Collection
The vehicle was equipped with the following sensors: pressure, light, conductivity, and temperature. A reading from each was recorded approximately every 30 seconds. The resulting data was calibrated and indexed by the depth
of the reading (as obtained using the pressure range and the depth range) to provide our final table of data.
Our team had one successful day of data collection, May 6, 2009 during lab hours (2-5 PM) at the MIT Sailing Pavilion, during which we obtained a maximum depth of 2.7 meters. We had a few bad readings, but the vast majority
of our data calibrated to at least somewhat logical results. Conductivity was consistently in the 1.75-1.85 S/m range whenever the sensor was in the water, and 0 or very, very close to it when it was not. At depths greater than half
a meter, 0.2-0.5% of the intensity of sunlight was recorded by our light sensor, whereas at 0.23 meters, about 4% was recorded. The temperature variation was not generally more than one or two degrees from 20 C, and showed
no discernable pattern.

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