AVIATION INVESTIGATION REPORT
A06A0115
LOSS OF CABIN PRESSURE
AIR CANADA JAZZ
CANADAIR CL600-2B19 C-FSJJ
FREDERICTON AIRPORT, NEW BRUNSWICK, 100 nm NW
03 NOVEMBER 2006
The Transportation Safety Board of Canada (TSB) investigated this occurrence for the purpose
of advancing transportation safety. It is not the function of the Board to assign fault or
determine civil or criminal liability.
Aviation Investigation Report
Loss of Cabin Pressure
Air Canada Jazz
Canadair CL600-2B19 C-FSJJ
Fredericton Airport, New Brunswick, 100 nm NW
03 November 2006
Report Number A06A0115
Summary
An Air Canada Jazz Canadair CL600-2B19 (serial number 7058, registration C-FSJJ) being
operated as JZA8954 was on a scheduled flight from Toronto, Ontario, to Fredericton, New
Brunswick. While in cruise at flight level 330, the flight crew observed the cabin altitude
climbing at a rate of approximately 1000 feet per minute. A descent clearance to flight level 250
was requested from Moncton Area Control Centre and, after the aircraft was level at
flight level 250, a continued increase in cabin altitude was observed. The crew requested and
received clearance for further descent to 9000 feet. The pilots donned their oxygen masks during
the descent as the cabin altitude climbed through 10 000 feet. When the cabin altitude reached
14 000 feet the passenger oxygen masks automatically deployed. The aircraft was leveled at
9000 feet where it remained until descent for final approach was initiated. The aircraft landed at
Fredericton without further incident at 2115 coordinated universal time. There were no injuries
to the 50 passengers and 3 crew members.
Ce rapport est également disponible en français.
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Other Factual Information
Modern commercial aircraft that are designed to conduct sustained flight above 10 000 feet are
pressurized. The pressurization systems are automatically controlled to maintain cabin altitudes
below 10 000 feet in order to provide a safe and comfortable environment for the passengers. As
the aircraft climbs, its pressurization system pumps air into the fuselage to maintain a cabin
pressure altitude below 10 000 feet. This results in a higher pressure inside the aircraft than that
of atmospheric pressure outside. The resulting pressure differential is regulated by the aircraft
system.
Before the pressure loss started, C-FSJJ was level at flight level (FL) 330 while maintaining a
cabin altitude below 10 000 feet. The aircraft had been established in level cruise flight for
approximately 16 minutes before the crew detected a cabin pressure variation. Although there
were no aircraft system warnings or caution messages present on the engine indicating and
crew alerting control system (EICAS), the crew noticed that the cabin altitude was climbing at
approximately 1000 feet per minute. On checking the air conditioning control panel, it was
observed that the left air conditioning unit (ACU) pack was on-line. However, the right ACU
pack was off-line. The bleed air control panel was indicating that the right 10th stage bleed shut-
off valve (SOV) was also off-line. Therefore, the left ACU pack was the only available source of
pressure for the air conditioning and pressurization demands of the aircraft.
If one of the two ACU packs goes off-line, the remaining pack will automatically switch to Hi
flow as a normal function of the system. This should ensure cabin pressure can be maintained at
an altitude below 8000 feet. The maximum aircraft altitude for single-pack operation is
25 000 feet.
After receiving clearance from Moncton Area Control Centre (ACC), the crew expedited descent
with the intent of leveling off at FL250 before the cabin altitude could reach 10 000 feet. During
the descent, the crew attempted to reset both the right 10th stage bleed SOV and the right ACU
pack but neither would come back on-line.
Once the descent from FL250 was initiated, the captain made an announcement informing
passengers that one of the ACU packs was not operating and that the flight was continuing on
to destination. Approximately one minute after descent was initiated, the master warning
illuminated for two seconds and the cabin altitude warning came on. The crew then observed
“DISPLAY COOL” and “AIRINC COOL” messages on the EICAS primary display.
During the descent from FL250, the cabin altitude warning activated indicating that the cabin
altitude had reached 10 000 feet. At this time the flight crew donned their oxygen masks.
Despite an average rate of descent of 4000 feet per minute, the cabin altitude climbed steadily
until it reached 14 000 feet. At that point the passenger oxygen masks deployed automatically.
The cabin altitude warning extinguished after the aircraft descended below 10 000 feet.
After the aircraft was level at 9000 feet, the flight crew ran through the associated checklists and
noticed that the pressurization fault light was illuminated on the pressurization panel. The crew
then selected manual pressurization mode.
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Seven days earlier, the aircraft was reported to have had poor airflow. Ground runs were
completed by the maintenance personnel; the airflow was reported as normal.
Following the occurrence flight, a maintenance inspection revealed several separate anomalies
related to both the left and right air conditioning systems:
The left system, air supply duct (part number 601R95211-113), was found detached
from its flange at the water separator joint. The duct is located in the unpressurized
tail section of the aircraft, aft of the pressure vessel. The detached flange created a
leak through which an undetermined percentage of air pressure was lost.
The right system pressure regulating shut-off valve (PRSOV) sense line was found
detached, which effectively caused that system to go off-line.
Both the right and left system bulkhead check valves (part number 92E20-4) were
missing a return spring. The missing return springs would permit the check valves to
remain open and allow cabin air to backflow and escape through the duct system in
the event of a breach in the respective ducts between the PRSOV valves and the
pressure bulkhead. The missing springs were not located.
The duct flange failure observed in the left system was similar in nature to previous duct
failures experienced in the air supply systems of the CRJ 100/200 series aircraft. Those duct
failures are the subject of an airworthiness directive (CF-2003-05R1). However, those ducts are
of a different part number and location within the air supply system than the duct that was
found detached on C-FSJJ.
Transport Canada Airworthiness Directive (AD) CF-2003-05 “Air Supply Ducts and Bulkhead
Valve – Inspections” was issued on 04 February 2003; this was later superseded by
CF-2003-05R1 issued on 31 March 2006. The background section of the AD indicates the
following:
The manufacturing procedure used to attach the flanges to the air supply
ducts has resulted in bonds that may lose shear strength at elevated
temperatures. This condition could potentially cause the duct to disconnect
and in combination with the failure of a bulkhead check valve, result in the
in-flight loss of aircraft pressurization.
Technical records indicated that no recent maintenance had been carried out on the PRSOV line.
The investigation could not determine how the line became loose and detached.
It should be noted that as part of AD CF-2003-05R1, Bombardier added a new task to the CRJ
maintenance program. The task calls for a repeat check valve inspection at an interval of
4000 flight hours. Prior to this incident, the check valves (part number 92E20-4) were last
inspected at the operator facilities on 08 August 2005; the springs were present and deemed
serviceable.
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Analysis
The most plausible initiating event related to the reduction in cabin pressure was the loose
PRSOV line serving the right air conditioning pack. Once the line had detached completely, the
actual duct pressure for the right ACU pack could not be sensed accurately and the PRSOV
valve likely closed. The closed PRSOV valve effectively caused the right pack to go off-line.
When either of the two packs goes off-line, the remaining pack will automatically switch to Hi
flow as a normal function of the system. In this case the left pack did switch to Hi flow, which
increased the pressure in that respective duct system.
The additional pressure from the Hi flow may have caused an already weak flange-to-duct joint
to fail completely. It is also possible that the duct had deteriorated over time and was already
partially detached from the flange. Normally, one air conditioning pack operating at Hi flow is
adequate for aircraft pressurization, provided a maximum aircraft altitude of 25 000 feet is
maintained. However, once the flange failed, duct pressure was reduced as the air escaped into
the unpressurized tail section.
The “DISPLAY COOL” and “ARINC COOL” EICAS messages the crew observed were most
likely triggered by a low airflow condition in ducts that supply cooling air to the instrument
panel and the avionics bay of the aircraft. The caution messages do not necessarily indicate a
higher than normal duct temperature. They do indicate the fact that a low airflow supply to the
instrument panel and to the avionics bay was resulting in an increased operating temperature of
those particular components. It is also possible for messages to be triggered by flow sensors in
the system that are sensitive to changes in air density as cabin altitude increases.
After the right air conditioning system had gone off-line and the left air conditioning system
became the sole source of air pressure to the cabin, the right bulkhead check valve should have
closed. However, the check valve remained open due to the missing spring. This allowed cabin
air pressure to backflow through the inoperative right system ducting up to the PRSOV valve
which had closed due to the detached PRSOV line. Had the bulkhead check valve spring been
in place, the valve would have closed when the duct pressure opposing it decreased. This
would have prevented backflow of the pressurizing air to the PRSOV valve. Since there was no
breach in the right system between the bulkhead check valve and the PRSOV valve, the cabin
pressure loss to ambient from the right side would have been negligible. The left bulkhead
check valve spring was also missing but in this case it had little effect on the rate of cabin
pressure loss since some supply air was likely available from the left ACU pack. The missing
check valve springs were not recovered and it could not be determined how long they had been
missing. The effect of a missing check valve spring would go unnoticed during normal
operation of the system and, therefore, could go undetected for some time. The left system duct
had detached at the water separator which effectively allowed the majority of supply air from
the left ACU to escape from the ducting.
Although the left air conditioning system continued to operate and supply the cabin/cockpit
with air pressure, the pressure supplied was insufficient to overcome the rate of pressure loss
created by the left system duct leak. Therefore, the cabin altitude could not be controlled and
continued to climb.
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The combined effect of the independent technical failures across both independent ACU pack
systems resulted in a loss of cabin pressurization. This loss of pressurization was not easily
detected as one pack remained on-line and in Hi flow mode. However, the majority of the
supply air pressure coming from the left pack was escaping through the dislodged duct flange
before it could enter the cabin. According to Bombardier analysis from other incidents, the rate
of pressure loss in this case was the same as what could be expected if there were little or no air
pressure entering the aircraft cabin, provided the following conditions are met: there is no
significant breach in the pressure vessel or the systems that supply pressure to the cabin, and
the aircraft pressure vessel has nothing more than the normal leak-down rate expected.
It is unusual for a flight crew to be faced with multiple, unrelated failures at the same time. In
this case the crew attempted to resolve the problem but it could not be rectified in flight. Due to
the lack of any other significant pressurization warnings and because the aircraft can normally
operate on one pack, the crew’s initial plan to descend to 25 000 feet was reasonable.
The following TSB Engineering Laboratory report was completed:
LP 109/2006 – FDR Analysis
This report is available from the Transportation Safety Board upon request.
Finding as to Causes and Contributing Factors
1. The combined effect of the detached left air conditioning unit pack system air supply
duct, the detached right system pressure regulating shut-off valve line, and the
missing return spring on the left system bulkhead check valve resulted in the loss of
cabin pressurization.
This report concludes the Transportation Safety Board’s investigation into this occurrence. Consequently,
the Board authorized the release of this report on 13 March 2008.
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