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Procedia Manufacturing 22 (2018) 886–892
Procedia Manufacturing 00 (2017) 000–000
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11th International Conference Interdisciplinarity in Engineering, INTER-ENG 2017, 5-6 October
11th International Conference Interdisciplinarity in Engineering,
2017, Tirgu-Mures, Romania INTER-ENG 2017, 5-6 October
2017, Tirgu-Mures, Romania
The contribution of lean manufacturing tools to changeover time
The contribution
Manufacturing of Society
lean manufacturing tools to MESIC
changeover time
decreaseEngineering 2017,
International Conference
in the pharmaceutical
Vigo industry.
(Pontevedra), Spain
2017,
A SMED 2017, 28-30
project. June
decrease in the pharmaceutical industry. A SMED project.
a, b c d
Al-Akel Karam
Costing models a, *, Marian
for capacity Liviub, Veres Cristina
optimization in Industryc, Horea 4.0:Radu
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P Petru Maior University of Targu Mures, Nicolae Iorga street, no. 1, Targu Mures, 540088, Romania
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1. Introduction
* Corresponding author. Tel.: +40-740-196-220; fax: +40-264-763-173.
* E-mail
Corresponding
address:author. Tel.: +40-740-196-220; fax: +40-264-763-173.
karam.alakel@gmail.com
The cost
E-mail of idle
address: capacity is a fundamental information for companies and their management of extreme importance
karam.alakel@gmail.com
in modern©production
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International Conference The management of the idle capacity
in Engineering.
Peer-review underTel.:
* Paulo Afonso. responsibility
+351 253of the761;
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fax: +351 253 604of741
the 11th International Conference Interdisciplinarity in Engineering.
E-mail address: psafonso@dps.uminho.pt
achieving a product into Value added (VA) and Non Value Added (NVA). The waste elimination principle is to
minimize the NVA and focus on the VA activities [1][2][3]. Obtaining fast results in the shortest period of time is
every company’s target, but which are the optimal methods in achieving this? Among other lean tools, the Single
Minute Exchange of Dies (SMED) may be a very efficient method for reducing inventory [4] and mainly CO times
in the production area between different batches, products or machine setups especially by converting internal steps
(while machine is stopped) into external ones (while machine is still running) and shortening the steps that remained
[5]. SMED assures a quick and efficient change from the currently running product to the next one.
The Changeover time is the amount of time spent between the last good piece of one product until the first good
piece of the next product. The paper aims to present the implementation sequence and level of importance regarding
Lean-SMED techniques at a pharmaceutical solids production site.
Nomenclature
Single Minute Exchange of Dies assures a quick and efficient change from the currently running product to the
next one. The Changeover time is the amount of time spent between the last good piece of one product until the first
good piece of the next product. This amount of time is spent on cleaning and changing the machine parts and setup
for next product. Appropriately implementing SMED improvement system may represent the key factor into a
rewarding batch size reduction objective, which would assure more flexibility and improved product flow in the
manufacturing area [5]. Single Minute Exchange of Dies described by Shingo [6] assumes that a Changeover should
take place in a single digit expressed time (under 10 minutes). Nowadays the techniques for achieving a single digit
Changeover time were acquired and implemented in the manufacturing areas in order to shorten and standardize the
downtime between two batches by implementing different tools and techniques [7]. By observing the current
methodology, separating the internal and external activities, streamlining the process of Changeover and
continuous training the major SMED steps will be achieved and implemented [5]. The expected results will return
an economic benefit reflected in an increased product output. Beyond the economic VA benefits, by decreasing the
Changeover time further NVA achievements such as better ergonomic conditions, standardization, teamwork and
workload are expected [8]. An integrated Overall Equipment Efficiency (OEE), a Key Process Indicator is expected
to be raised by decreasing the equipment downtime lost with Changeover [9], [10], [11].
The targeted company for applying the SMED project had a current need for shortening CO times at a certain
production line. At the bottle filling machine are working 2 FTEs and a number of 37 CO processes had to be
conducted each year with a mean CO time of 25,3 hours. The set target was reducing this time to 16 hours (37%
decrease) by implementing Lean Manufacturing – SMED tools in order to shorten CO time, stabilize and reduce the
standard deviation of the process [2][12][13][14].
The up mentioned steps being achieved the reliability of the process will increase, an important financial gain
will be obtained and production planning will increase in stability.
888 Al-Akel Karam et al. / Procedia Manufacturing 22 (2018) 886–892
Al-Akel Karam et al. / Procedia Manufacturing 00 (2018) 893–899 895
The total savings will add up us soft ones with production equipment downtime loss and production labor by a
better Full Time Equivalent (FTE) distribution. The saving calculation result was expressed in financial figures
depending on cost/hour of FTEs and production equipment [15].
4. Implementation steps
Implementation steps followed the DMAIC structure in order to successfully implement the SMED methodology
[6], [16]. The Define phase being completed, a measuring upon the current process state had to be done in order to
reveal the current and real process status.
The specific Changeover times and data until the project start were collected for the past year from an Electronic
Manufacturing Software (EMS). Current working method in the Changeover process was collected through Gemba
walks and by one-on-one discussions with all the members involved in the process. Storage of the collected data was
kept in Microsoft Excel/Microsoft Word software and processed in Minitab 17. The initial one on one discussions
were documented on paper base, being later transposed into the up mentioned electronic software’s for a better
traceability and storage.
a b
Through analysis of the collected data (Baseline capability) in Fig. 1. (a) a significant standard deviation (σ) of
the individual CO times from the process mean can be observed concerning upon a lack of process standardization.
Fig 1. (b) expresses the oscillations of individual CO times, instead of an aggregation. Through Gemba walks and
discussion with the directly implied personnel in the CO process the major root causes were identified.
A critical aspect in being able to bring an improvement to a certain process or a workplace is the ability of
correctly identifying the problems and deficits involved in achieving your goals and targets through the current
process state. In Table 1 we displayed the main root causes established after using the Gemba walk tool and
interviewing the implied personnel.
The most important element in conducting an improvement process is to correctly identify the root causes of your
wastes. Once root causes were identified the team proceeded in finding and implementing the optimal improvement
methods for the process.
4.2. Improvement
For each root cause a proper improvement has been found and implemented on the shop floor. Not only by
analyzing the data collected until this step, but also through Gemba walks, brainstorming and regular meetings
proper solutions were identified.
a b c
Fig. 2. Visual management on the shop floor area for bottle filling machine: (a) tools cabinet; (b) product storage; (c) packaging materials.
Targets were set and controlled through visual boards displayed on the shop floor, visual boards were printed by
the project leader, problems being discussed after each CO and collected in an electronic database.
• FTE redistribution demand
The bottleneck process was represented by the CO in the primary packaging area, in order to assure a proper
work force additional 2 persons had to be assigned for helping in the process. Each person had exact tasks controlled
with the major CO scheme and CO step time, being possible to execute simultaneous steps.
As part of the project, the primary packaging storage was redesigned and moved closer to the bottle filling room
in order to shorten the travelled distance for bringing the needed materials by 100 meters. Travel time decreased
from an average of 4 minutes to 2 minutes.
The involvement of operators is critical for the Changeover process, participating with ideas and implementing
the best ones is a key factor for the success of Lean Manufacturing shop floor implementation. The criteria’s that
have to be taken into consideration are regarding the limitations of the process and implementation area. Lean
Manufacturing tools have to be adapted to each work place in particular, taking into consideration its design and
needs. Finding the optimal tools and techniques to implement most effectively Lean Manufacturing on a shop floor
level is the responsibility of the project leader.
As a result of implementing Lean Manufacturing – SMED techniques on the production shop floor in the bottle
filling Changeover process the process mean changed significantly. From a mean CO time of 25,3 hours a
significant decrease was obtained down to 17,8 hours (30% decrease). From Fig. 3. (a) it is possible to distinguish
the fact that the after CO mean time and standard deviation from the mean have decreased. Fig. 3. (b) graphically
represents the decrease in time and variation of the CO after project implementation. In Figure 4 we have displayed
the results obtained under the Boxplot chart form for a clearer perspective. In this particular case a single digit
Changeover is extremely hard to achieve and a 30% improvement is considered an essential one. Nevertheless, the
control phase and further improvement of the Changeover process will continue until being able to maintain mean
process duration of 16 hours.
As a result the saved time by eliminating process wastes will facilitate the output increase of yearly packed
bottles returning financial benefits if the machine is stocked with orders. The indirect benefits of the SMED project
will display in increased process standardization, higher customer satisfaction reflected by improved flexibility of
Changeovers, finer teamwork and a better FTE distribution.
A need of better communication between operators and between operator-supervisor was identified in order to
implement a successful Lean Manufacturing technique. Communication, discipline and process control are the core
elements into succeeding in continuous improvement.
Al-Akel Karam et al. / Procedia Manufacturing 22 (2018) 886–892 891
898 Al-Akel Karam et al. / Procedia Manufacturing 00 (2018) 893–899
a b
Fig. 3. (a) Process performance capability report Before/After (b) Diagnostic capability report on CO Time Before/After.
6. Conclusion
Taking into consideration the need to keep up with a global trend of product customization and cost reduction
requirements the most effective use of resources has to be assured in every working area. The flexibility from one
product to another is ensured by a Changeover process which has to be as efficient as possible to be able to meet the
customer demand and productivity targets. Single Minute Exchange of Dies involves a methodology, certain
techniques and tools in order to perform a more quick and efficient Changeover, positively influencing flexibility
and product output [21][22].
Single Minute Exchange of Dies methodology was adapted and used to improve the Changeover process at a
bottle filling line in the pharmaceutical industry. Being guided by the SMED methodology the desired result was
nearly achieved within an implementation period of six months. In the control phase further improvements are
expected and the main scope being the reduction of CO time to the initial target of 16 hours.
Properly adapting and using only the key tools from LM arsenal for the needed implementation area will count in
obtaining the most Value Added outcomes. Results obtained through SMED by externalizing steps, visual
management and FTE redistribution as major change categories led to standard and efficient Changeover process
with a 30% decreased completion time. The removed CO wastes and shortened completion time will assure a greater
product output/time unit bringing important financial savings to a targeted group. A clear improvement can be
brought by implementing Lean improvement tools in the manufacturing area; the key factor is choosing the right
ones to start with.
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Al-Akel Karam et al. / Procedia Manufacturing 00 (2018) 893–899 899
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