8D -CORRECTIVE ACTION REPORT
Date Initiated: September 05, 2019                              Date Revised: --
CAPA report :                                                   Inspection report issue date: August 26, 2019
Supplier Name: PT. Rubber Jaya Lampung                          Part description:
Supplier Contact: Mr. Oei Yohanes                               Issuer at ----
Rejected quantity -                                             Rejected Quantity after investigation:-
 Recurrent issue?        Customer safety effect
                                                                                                                  Responsible
D1: Use a Team Approach
The Problem Solving Investigator uses a multi-person approach to collect information from those directly
associated with and/or impacted by the problem. The Team members’ names and contact info should be               Benny Indra
listed here.                                                                                                       Royani
                 Team Members:                                        Business Phone:                            Planned date
Novia Ika Z.                                                           082386539800
                                                                                                                 April 30, 2019
Septia Yolanda                                                         085879265998
                                                                                                                 Achieved date
Cika Ratih                                                             0895352278707
                                                                                                                May 8, 2019
Yustinah                                                               0895341524340
                                                                                                                  Responsible
D2: Describe the Problem
.                                                                                                               Benny Indra R
WHAT is the problem in comparison to a conforming part?
Contamination visible on bales
WHY is it a problem? Explain the effect.
Contamination found in bale that out of trolley like volcanic and wood contamination occurs because the
sorter / QC cannot see the presence of volcanic acid in the raw material, control of the raw material
rotation process.
WHEN was the problem discovered?          WHERE?             BY WHO?
On 6 August 2019 when wet-dry production is discovered by sorters and QC officers.
HOW was it detected?
Do check of raw materials on conveyor and bale on trolley
HOW MANY defective parts have been detected?
Just one bale
Are other part numbers affected?     YES     NO
                                                                                                                 Achieved date
                                                                                                                May 8, 2019
D3: Implement and Verify Containment (temporary fix)                                                    Responsible
Implement containment to control the situation and mitigate further negative effects of the
problem. (Segregation, selection, temporary actions in the process etc…..)
                                     8D -CORRECTIVE ACTION REPORT
                                                                                                               Benny Indra R
 How – Provide work instruction for sorter on raw materials and for contamination taker. Provide visual
 control for contamination and do random check for bales. 2 pallet after dunnage each shift, check all
 bale surface, all layer. If we find contamination indication, will do addition checking for 5 pallet before
 and 5 pallet after.
 Where – on sorting of raw materials, Conveyor and Washing tank on wet process and Vibrating
 screen on Dry Process.
 Who – By sorter on raw materials, contamination taker and Quality Control Checker
 When – for raw materials to check contamination when the supplier of raw materials will send it
 materials. For Conveyor and Washing tank on wet process and Vibrating screen on Dry
 Process to check more throughly.
 Check –Working inspection for sorting of raw materials and provide visual control for contamination
 and do random check for bales.
 Markings on delivered OK parts? :
                                 Sorting results at each step of the flow
         Location               Material   Sorted                    Quantities/Comments
  Customer Plant:               YES        NO
  Warehouse & Transit:          YES        NO
  Supplier Plant:               YES        NO
                                                                                                                Achieved date
 What have we learned from the sorting?                                                                         May 8, 2019
 To inspect more seriously our product
D4: Root Cause Analysis                                                                                          Responsible
Identify the Possible Causes of the problem for both occurrence and non detection. Conduct a
Root Cause Analysis to determine true Root Cause of the problem using the 5Whys. Reproduce                     Benny Indra R
the defect to confirm the true root cause.
 Occurrence: 5 W +Proof                                                                                          Planned date
 Aspect         Contamination clearly visible on bales                                                         April 30, 2019
 Why            Less control from sorter on raw materials
 Why            Less control from contamination taker on Conveyor and Washing tank at wet
                process
 Why            Less control from contamination taker on Vibrating screen at Dry Process
 Why            Less control from Quality Control Checker on bales
 Who            sorter of raw materials , contamination taker and Quality Control Checker                       Achieved Date
 Proof          Attach 1 work instruction for sorting of raw materials, Attach 2 Training List,                 May 8, 2019
                Attach 3 Contamination Visual Control, Attach 4 Training list, Attach 5 work
                instruction for take a contamination on wet process, Attach 6 Training list, Attach
                7 work instruction for take a contamination on Conveyor, Attach 8 Training list ,
                Attach 9 work instruction for take a contamination on Vibrating screen, Attach 10
                Training list, and Attach 11 work instruction for take a contamination on bales.
 D5: Develop Permanent Corrective Actions / Solution(s)                                                          Responsible
 Develop Permanent Solution(s) that address each Root Cause. Verify and test the Permanent
                                                                                                               Benny Indra R
 Solution(s).
 Occurrence (How ,where, Who, When, Check)                                                                       Planned date
 Aspect       Contamination clearly visible on bales
                                                                                                               April 30, 2019
 How          Provide work instruction for sorter on raw materials and for contamination taker . Provide
              visual control for contamination and do random check for bales. 2 pallet after dunnage
              each shift, check all bale surface, all layer. If we find contamination indication, will do
              addition checking for 5 pallet before and 5 pallet after
                                  8D -CORRECTIVE ACTION REPORT
                 -   On sorting of raw materials,
                 -   Conveyor and Washing tank on wet process
 Where
                 -   Vibrating screen on Dry Process.
 Who        sorter of raw materials , contamination taker and Quality Control Checker
            for raw materials to check contamination when the supplier of raw materials will send it
            materials. For Conveyor and Washing tank on wet process and Vibrating screen on
 When
            Dry Process to check more thoroughly and Quality Control checker on bales every
            hours.
            Working inspection for sorting of raw materials and provide visual control for
 Check
            contamination and do random check for bales.                                                   Achieved Date
                                                                                                          May 8, 2019
 D6: Validate Permanent CA / Solution(s)                                                                    Responsible
 Validate that the chosen solution is effective.
                                                                                                          Benny Indra R
 - work instruction for sorting of raw materials
 - Visual Control Contamination
                                                                                                           Achieved date
 - Work instruction for take a contamination on wet process,
 - Random check for bales                                                                                 May 8, 2019
 D7: Prevent Recurrence                                                                                     Responsible
 Prevent recurrence of the problem at the problem site and across the organization.
                                                                                                          Benny Indra R
Standards update (PFMEA, control plan, work instructions, maintenance plan, procedures….)                   Planned date
(What, Who, When, Submit update
Aspect         Contamination clearly visible on bales
                - Provide work instruction for sorter on raw materials and for contamination taker
What            - Provide visual control for contamination
                - Provide work instruction for pallet separation check                                    April 30, 2019
Who            By sorter of raw materials , contamination taker and Quality Control Checker
               for raw materials to check contamination when the supplier of raw materials will send it
               materials. For Conveyor and Washing tank on wet process and Vibrating screen on
When                                                                                                       Achieved date
               Dry Process to check more thoroughly and Quality Control checker on bales every
               hours.
                                                                                                           May 8, 2019
Holistic View/Generalization
 Can this problem occur on a similar product?
 Can this problem occur on a similar line?
    Who is assigned to address this issue?
                                                                                                            Responsible
 D8: Close Problem and Recognize Contributions
                                                                                                          Benny Indra R
 Audit implemented solutions. (when, result) Reinforce the 8D process with recognition of team
 member contributions.
                                                                                                            Planned date
 Ok. No more problem occure after Corrective Action. Implement since March-May 2019.                      April 30, 2019
                                                                                                           Achieved date
                             8D -CORRECTIVE ACTION REPORT
                                                                                             May 8, 2019
OPTIONAL
The undersigned have verified acceptable corrective action effectiveness on the above stated corrective
actions:
   Supplier Representative Responsible                       Signature                         Date
Name/Title: Benny Indra Royani                                                              May 8, 2019
Name/Title:
Revision History
     Rev. no              Rev. Date         Reason for change
       00                  31.12.15         New Release
       00                  25.08.16         Updated for IMS Edition 03
        01                05.03.18          Updated for R&D WI
               Prepared By                           Reviewed By                       Approved By